陈廷官, 张宏文, 王磊, 张龙唱, 王军, 李建新, 谷艳清. 水平摘锭式采棉机采摘头传动系统优化与试验[J]. 农业工程学报, 2020, 36(17): 18-26. DOI: 10.11975/j.issn.1002-6819.2020.17.003
    引用本文: 陈廷官, 张宏文, 王磊, 张龙唱, 王军, 李建新, 谷艳清. 水平摘锭式采棉机采摘头传动系统优化与试验[J]. 农业工程学报, 2020, 36(17): 18-26. DOI: 10.11975/j.issn.1002-6819.2020.17.003
    Chen Tingguan, Zhang Hongwen, Wang Lei, Zhang Longchang, Wang Jun, Li Jianxin, Gu Yanqing. Optimization and experiments of picking head transmission system of horizontal spindle type cotton picker[J]. Transactions of the Chinese Society of Agricultural Engineering (Transactions of the CSAE), 2020, 36(17): 18-26. DOI: 10.11975/j.issn.1002-6819.2020.17.003
    Citation: Chen Tingguan, Zhang Hongwen, Wang Lei, Zhang Longchang, Wang Jun, Li Jianxin, Gu Yanqing. Optimization and experiments of picking head transmission system of horizontal spindle type cotton picker[J]. Transactions of the Chinese Society of Agricultural Engineering (Transactions of the CSAE), 2020, 36(17): 18-26. DOI: 10.11975/j.issn.1002-6819.2020.17.003

    水平摘锭式采棉机采摘头传动系统优化与试验

    Optimization and experiments of picking head transmission system of horizontal spindle type cotton picker

    • 摘要: 为了提高水平摘锭式采棉机的作业效率,针对国产采棉机在高速作业过程中存在采摘速比系数匹配不当、采摘头传动系统不合理的问题,该研究根据水平摘锭式采棉机采摘头结构与工作原理,对采摘头传动系统、采棉机采摘机理进行分析,根据传动系统传动要求和采棉机采摘条件,建立目标函数与约束条件,运用遗传算法和1stOpt软件对采摘头传动系统进行优化分析。优化结果为:滚筒动力齿轮齿数为72,离合器上齿轮变位系数为-0.14,滚筒动力齿轮变位系数为1.208,齿轮顶隙系数为1.25。结合采棉机作业要求搭建棉花采摘性能试验台,选取采摘滚筒转速113~143 r/min、作业速度5.93~7.20 km/h,对优化前后采摘头的作业性能进行验证试验。结果表明:优化后的采摘头作业速度由6.4 km/h提升至7.2 km/h,工作效率由4.86 hm2/h提升至5.47 hm2/h,提高了12.5%;优化后的采摘头在7.2 km/h的作业速度下,采净率由90.4%提升至93.7%,采净率提高了3.6%,含杂率由10.28%降至9.72%,含杂率降低了5.4%,验证了传动系统优化结果的合理性。该研究可为国产采棉机采摘头的研发提供参考。

       

      Abstract: Cotton is an important strategic material. With the increase of cotton planting costs, improving the level of mechanized harvesting has become an important way to improve the economic benefits of cotton planting. The main cotton harvesting machinery used in China is the horizontal spindle type cotton picker. In the process of production practice, the domestic cotton pickers have problems during high-speed operation, such as improper matching of picking speed ratio coefficient, badly gear worn and poor reliability of picking head transmission system. In view of the above problems, this paper optimized the transmission system of picking head based on the comprehensively consideration of the operating speed, transmission system reliability, operation quality and other factors, aiming to increase the operating speed of the cotton picker, improve the reliability of the picking head transmission system and the operation quality of picking head. According to the structure and working principle of the horizontal spindle type cotton picking head, the transmission route and transmission ratio of picking head transmission system of cotton picker were analyzed and calculated firstly. Then, the picking mechanism and picking conditions, such as the range of picking speed ratio coefficient of cotton picker, the actual number of turns needed to pick cotton petals and the picking time of spindle, were determined through virtual simulation technology and theoretical analysis and calculation. Meanwhile, the roller power gear in the transmission system of the picking head was selected as the optimization object, the tooth number of roller power gear, modification coefficient of the upper gear on clutch, modification coefficient of roller power gear and addendum height coefficient were selected as design variables, and the objective function and constraint conditions were established. The Genetic algorithm and 1stOpt software were used to optimize the transmission system of picking head. The optimization results were as follows: the number of teeth for the roller power gear was 72, the modification coefficient of the upper gear on the clutch was -0.14, the gear modification coefficient for the roller was 1.208, and the addendum height coefficient was 1.25. A cotton picking performance test bench was built combining the operation requirements of the cotton picker. The operation performance of picking head before and after optimization was verified on the test bench with the factors as follows: picking roller speed was 113-143 r/min, the operation speed was 5.93-7.20 km/h. The results showed that the working speed of the picking head was increased from 6.4 to 7.2 km/h, increased by 3.6%, and the work efficiency increased from 4.86 to 5.47 hm2/h, increased by 12.5%. Under the working speed of 7.2 km/h, compared with before optimization, the collection rate increased from 90.4% to 93.7%, increased by 3.6%, and the impurity rate decreased from 10.28% to 9.72% and decreased by 5.4%, which verified the rationality of the optimization of the picking head transmission system in this paper. The study can provide a reference for the development of picking head of cotton picker.

       

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